Had a 039 in a long time ago, it had been seized so fitted a new piston etc and it ran but not too great. Found the carb was a bit worn so fitted new and it ran a lot better. Compression was never great - 150 tops but adequate.
Well......this saw came back, reset the carb and back out, failed, came back, went out....well, you have the picture. This saw was the spawn of the Devil and nothing would sort it.
I felt guilty that it wasn't right, that is just the way I am, I don't like taking money and the customer not having a working saw so had it back after I ported a 372 for the fella and said it may be a long project.
Well - I tore in to it this week, measured the squish, stripped it down again, found a slight abrasion to the piston so smoothed and re-honed the cylinder. Everything else seemed OK. I compared the roof of the exhaust port distance to the squish band and it is significantly less than other cylinders I had to hand so now understand why the compression wasn't higher.
Found the flywheel had been rubbing on the plastic behind it so eased both plastic and flywheel to give clearance. pressure and vacuum check. Stripped the carb and there it was. A tiny sliver of wood stuck in the low speed jet pickup:001_rolleyes: No wonder the damn thing never idled well and was a bitch to start! The carb was a new one so never really checked it thoroughly - my mistake.
Went at a big lump of conifer, lots of noodling and it works fine and starts with no effort at all - months of hassle over:thumbup:
I won't charge, I got paid for the first repair and that usually does it on 99.9% of machines and will take this one on the nose. Just glad I got it sorted at long last.