I'm still wrong and you're right it's the pump diaphragm I've been calling the reed.
Gaskets checked and in the correct order, i tried flipping the metering diaphragm and it may have made it a fraction better but after a reset its the same
The fuel line, filter and tank were all given a really good clean, its on the standard white filter but running it with a much less restrictive filter its the same. I don't have a way to pressure test the fuel lines other than with my mouth and some carb cleaner and it seems ok.
I've opened up the exhaust outlet so when i blow through it the resistance feels about the same from each end so about twice the original size, it definitely sounds a lot happier and feels a bit more aggressive but no idle.
There's continuity on the red and yellow wires from the coil to the carb connector, i couldn't see where the black one terminated and completely forgot to check the carb side of it so will have to keep you posted on that one. I thought someone said a wiring fault is either intermittent or just wont work, my issue is consistent no matter how much i prod and poke those cables.
The flywheel gap is about .2-.3mm, my feeler gauge has seen better days but what should the gap be?
The plug spur is well connected and doesn't look yanked, it has a reassuring click and again holding it in or wiggling it around it runs the same. There's a slight dint in the HT lead where the retaining screw has compressed the plastic and i cant check the rest of it without removing the fly and i need to make a puller for that.
The spark isn’t really saying too rich or lean it was possibly a bit rich on the no6 plug so I put a no7 in it and seems possibly a little lean now but well within old carb parameters on both
Thanks, I know I shouldn’t do it but I feel a bit stuck because with a standard carb id just up the idle and or adjust the L on the carb and it would either give me something to work from or just work again but I can’t do that with this one other than forcing it with the idle set screw on the carb which is fine for a while but the mtronic seems to learn and the problem reoccurs and I up it a bit more to the point where when I set it back to “factory” after the full carb clean the screw was nearly 3 turns out so clearly not a solution.